Page 2 of 2 FirstFirst 12
Results 21 to 28 of 28

Thread: Will a 180V DC Motor Turn with 60V DC going into it?

  1. #21
    Senior Member
    Uncle Fester's Avatar
    Join Date
    Jan 2008
    Location
    Commonly found in a pantry or the bottom of a fridge, searching for grains, fermented or distilled
    Posts
    6,417
    Thanks
    2,293
    Thanked 4,421 Times in 2,522 Posts
    Rep Power
    2050
    Reputation
    81918

    Default

    Quote Originally Posted by hinekadon View Post
    there are brushless dc motors !!! when i was going thru training in 1960s the tutor bought in a lucus dc motor that had a rotor made of a series of bar magnets and field windings on stator unusual in those days but still brushless (and gutless from memory )lol
    The field windings would have to be powered by an alternating current or a series of pulses, NOT DC !
    Every step motor works like that too. You might be providing a DC but there is some sort of configuration that converts it.

    Brushless DC motors all require some kind of external circuit.
    Last edited by Uncle Fester; 04-08-18 at 03:15 PM.
    Update: A deletion of features that work well and ain't broke but are deemed outdated in order to add things that are up to date and broken.
    Compatibility: A word soon to be deleted from our dictionaries as it is outdated.
    Humans: Entities that are not only outdated but broken... AI-self-learning-update-error...terminate...terminate...



  • #22
    Premium Member

    Join Date
    Jan 2010
    Posts
    1,077
    Thanks
    632
    Thanked 307 Times in 181 Posts
    Rep Power
    301
    Reputation
    4640

    Default

    Hi Guys,
    First I have to aplogise.
    I actually did not believe in hinekadon's reply about gluing the magnets. However, I was wrong and my previous post was a tad sarcastic. My apologies to hinekadon.

    My last post was misleading and incorrect. I did however, have every intention of telling what really happened, and had no idea that other people would respond about 'gluing'.
    The magnets were not loose.

    The fault was elsewhere. A very simple fault. Only taking apart the motor would have shown what was wrong.

    I include some photo's and the last one (Full Motor Showing) - to the keen eye - will show what was wrong.

    Top Off Motor.


    Magnets.


    Brushes with lots of wear to go.


    Opened Motor with fault Showing.


    Once again my apologies for being ignorant to hinekadon and others who tried to help on that 'glue' issue.


    GT250.

  • The Following User Says Thank You to GT250 For This Useful Post:

    BCNZ (05-08-18)

  • #23
    Banned

    Join Date
    Jan 2017
    Location
    still above ground level
    Posts
    1,779
    Thanks
    5,562
    Thanked 1,964 Times in 714 Posts
    Rep Power
    0
    Reputation
    35657

    Default

    so what are you going to do with it /?as it is repairable if you know how ? do you want to know or not ???

  • #24
    Premium Member

    Join Date
    Jan 2010
    Posts
    1,077
    Thanks
    632
    Thanked 307 Times in 181 Posts
    Rep Power
    301
    Reputation
    4640

    Default

    The Negative connection had come loose, as in the last pic.
    Simply soldered it back on and done!

    Obviously a bad solder and I guess the vibration over time did the trick.

  • #25
    Banned

    Join Date
    Jan 2017
    Location
    still above ground level
    Posts
    1,779
    Thanks
    5,562
    Thanked 1,964 Times in 714 Posts
    Rep Power
    0
    Reputation
    35657

    Default

    they are spot welded on manufactuer solders fine

  • #26
    Senior Member
    loopyloo's Avatar
    Join Date
    Feb 2008
    Location
    Mid North Coast NSW . Australia
    Age
    67
    Posts
    2,208
    Thanks
    1,431
    Thanked 470 Times in 314 Posts
    Rep Power
    416
    Reputation
    7317

    Default

    Better get rid of the carbon between the poles too, before you end up with a short.
    Just scrape it out gently with a fine pointed object.

  • The Following User Says Thank You to loopyloo For This Useful Post:

    GT250 (05-08-18)

  • #27
    Premium Member

    Join Date
    Jan 2008
    Posts
    4,311
    Thanks
    5,982
    Thanked 4,171 Times in 1,771 Posts
    Rep Power
    1349
    Reputation
    50392

    Default

    Good advice from Loopyloo.

    We always used a suitably shaped piece of broken hacksaw blade for the purpose of undercutting the insulating material which separates the commutator segments.

    We also dressed the commutator (rotor) surface by placing the commutator shaft in the chuck of a pedestal drill, rotating it at slow speed while holding a strip of very fine emery paper against the commutator surface to thoroughly clean and polish it.

    (Use a lathe for this purpose if dressing/polishing the commutator from a larger motor to avoid bending the shaft).

    Finally, visually inspect the commutator surface after this operation in order to make sure that there are no metal shavings shorting the commutator segments,

    Bush type bearings, where possible, were soaked for some hours in warm machine oil in order to lubricate them. (The purpose of warm oil was to ensure that the bearing soaked up the oil as they tend to dry out with prolonged use.

  • The Following 2 Users Say Thank You to tristen For This Useful Post:

    hinekadon (06-08-18),loopyloo (06-08-18)

  • #28
    Senior Member BCNZ's Avatar
    Join Date
    Jan 2008
    Location
    In the back of a 50 kW AM broadcast transmitter
    Posts
    1,697
    Thanks
    235
    Thanked 292 Times in 190 Posts
    Rep Power
    305
    Reputation
    2546

    Default

    The burning on the commutator is typical of what I was seeing with these motors.
    The brushes are very soft and arc up easily when the motor has too much load on it.
    I don't think the copper on the commutator is particularly good quality either.
    The design concept with these machines is OK, but like a lot of china sourced stuff it was let down by cheap componentry.
    I found that with the electronic controller units, once I'd been through them and replaced all the problem components with good quality parts, they gave no more trouble.

  • The Following 2 Users Say Thank You to BCNZ For This Useful Post:

    hinekadon (06-08-18),loopyloo (06-08-18)

  • Page 2 of 2 FirstFirst 12

    Bookmarks

    Posting Permissions

    • You may not post new threads
    • You may not post replies
    • You may not post attachments
    • You may not edit your posts
    •